1967, a standard 1967 289 V8 Mustang convertible.
2005, a 1967 289 V8 Mustang convertible with Don Berry Classics for a full “Eleanor” Restomod update.
2012, 20 June, serviced at Engine power by Performance Associates. Remove intake manifold and check surfaces, resealed with proper gaskets. Replace intake gaskets, upper radiator hose, spark plugs, and coolant. Test crank and cam sync sequence position. Found Hall Effect cam sensor incompatible with management system. Implement MSD Ignition with Hall Effect cam sync and re-calibrate to -1 - 1. After verification of crank and cam sync for sequential COP system, started vehicle with reasonable success. Very hard to start initially, uneven cranking and traces of backfire. Re-sync throttle bodies and re-engineer vacuum support to map sensor. Re-write calibration and re-start. Final sync throttle bodies and prepare for chassis Dyno. Work with cold start issues. Total invoice: $3,950.91.
2012, 14 Dec., serviced at Engine power by Performance Associates. Removed rack and pinion steering assembly, cross member, oil pan assembly and rear main cap. After removing the complete rack and pinion steering assembly to remove oil pan found that engine has a one-piece rear main seal. Found existing oil pan gasket was split causing oil leak around pan rails. Re-assembled with rubber/steel one-piece oil pan gasket. Performed oil and filter change. Eliminate existing toggle switch power circuit for Big Stuff 3. Necessary to fabricate new relay circuit from starter solenoid to ignition switch/P.C.M. switched power. Splice, solder and insulate wiring. Prove out system. Necessary to remove transmission and clutch assembly to properly install one-piece rear main seal. While transmission was out, re-sealed three oil galley plugs in back of engine block. Found bellhousing was too wide, necessary to trim both sides and top in order to re-install without taking the headers off. Cut out exhaust restrictors at tail pipe flanges for better flow and installed new flange gaskets at tail pipes. Re-build and re-seal clutch master cylinder as needed. Corrected ground at fuel pump circuit. Installed fuel pump relay and fuse under dash. Proved system, good. Total invoice: $2,764.77.
2012, 28 Dec., serviced at Glen’s alignment. Oil leak found at rear of engine, possible rear main seal. Remove steering assembly, cross member, oil pan assembly, rear main cap and replace rear main seal. Re-assemble components. Process necessary to facilitate ignition system and powertrain management system to operate using only the ignition switch. Eliminate existing toggle switch power circuit for Big Stuff 3. Necessary to fabricate new relay circuit from starter solenoid to ignition switch/P.C.M. switched power. Splice, solder and insulate wiring. Prove out system. Tachometer is non operable. Run Big Stuff green wire in loom and connect to tachometer. Verify signal is recognized. Replace batteries. Total invoice: $3,578.92.
2013, 03 June, serviced at Gran Prix Tire. Four new tires. Total invoice: $640.
2013, 21 June, serviced at Glen’s alignment. Charge battery and check no start. Check wiring for blown fuses or malfunctioning relay, check harness and computer charge batteries overnight on slow charge. Remove passenger seat and front carpet to remove and fix computer. Total invoice: $3,195.62.
2013, 19 July, serviced at Russo and Steele, LLC. Complete detail and prep, replace both tail lamp lens. Total invoice: $550.00.
2014, 05 Feb., serviced at JGM Automotive Tooling Inc, Motec systems USA. M84 ECU w/ log and single lambda, M84 1-LA UPGR SNGL to dual Lam s/n 29521, M CDL3 MX00 adapter loom. Total invoice: $1,087.40.
2014, 17 Feb., parts purchased at Sakata Motorsport Electronics, Inc., Injector, EV-14:051. Total invoice: $386.54.
2016, 10 Jan., serviced at Francorchamps of America Inc. Remove existing 2005 Big Stuff 3 engine management system system, wire in Motec, remove throttle bodies for rebuild, replace most of the front to rear fuel lines, rebuild throttle bodies, install check valve in fuel system, dyno car, replace brake lines with hard lines, replace master cylinder and electric brake booster, replace broken rear link, pull dash and replace speedo and water temp gauge have Shelby faces transferred, wire car for automatic fans, send out for alignment, install front tower brace, water jet engine compartment plate to expose vin, Replace batteries, find draw behind dash and remove unneeded relays, remove old and install new wiring harness, Labor. Total invoice: $38,659.14.
2016, January, for sale by Ferraris-online LLC. |